View in Other Languages Buccaneer Energy Limited (ASX:BCC) Kenai Loop气井测试进展更新 Buccaneer Energy Limited (ASX:BCC) Kenai Loop氣井測試進展更新 Buccaneer Energy Limited (ASX:BCC) Kenai Loop Testing Update 
Kenai Loop Testing Update
Kenai Loop Testing Update

Sydney, Dec 12, 2012 AEST (ABN Newswire) - Buccaneer Energy Limited (googlechartASX:BCC) advises that the process of identifying the location of the small leak in the well liner has progressed. The small leak was detected while checking pressure integrity of the casing and liner in anticipation of the start of perforation and production testing operations.

The leak identification process is one of trial and error within the full length of the casing and liner, progress has been made in narrowing the area where the leak exists. Once identified the plugging of the leak is a straightforward process of squeezing either fine cement or a polymer mixture into the leak to create a seal.

Once the leak is plugged and the casing and liner are successfully pressure tested it will take approximately 2-3 days to commence perforation and production testing. The Company will make a further release when the leak has been plug and the casing and liner have been successfully pressure tested.

The length of the casing and the cold conditions (-15oC) makes the repair process longer than what would be normally expected for what is a standard issue for operations of this type.

Background

Wire line logging of the Kenai Loop # 4 well has identified multiple sands with indications of gas within the Tyonek Formation. This includes 5 separate sands that have an average thickness of 34' each ('A' Zones) and that compare in quality to known productive sands in the Cannery Loop field that adjoins Kenai Loop, with each of these sands having gas shows while drilling. Further testing is needed to confirm these zones can be commercially produced as they were at Cannery Loop, the Cannery Loop field has produced 180 BCF (30 MMBO).

Additionally the equivalent 9,700' and 10,000' zones that are productive in the Kenai Loop # 1 well and producing a combined 6.5 MMCFD (1080 BOEPD) were also encountered in Kenai Loop # 4 well with both of these zones having very good gas shows while drilling. The 3D seismic indicates these sands are continuous from the Kenai Loop # 1 well to the south-east. In the Kenai Loop # 4 well, the 9,700' sand is 24' thick and the 10,000' sand is 76' thick.

Additionally the Kenai Loop # 4 well has also encountered several additional sands that appear to be gas bearing ('B' Zones), but do not compare with known productive sands in either the Cannery Loop or Kenai Loop fields.


Contact

Buccaneer Energy Limited
T: +61-2-9233-2520
F: +61-2-9233-2530
WWW: www.buccenergy.com



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